Reduced Downtime by 35% in a Multi-Line Packaging Facility

Results Snapshot

Downtime Reduction

-35%

Throughput Stability

Significantly Improved

Operational Impact

Higher Schedule Adherence

Challenge

Production output fluctuated heavily between shifts due to manual tracking, inconsistent reporting, and lack of real-time performance visibility.

Approach

  • Implemented real-time stop detection and automated downtime logging.
  • Standardized shift dashboards with live KPIs and loss tracking.
  • Introduced short-interval control meetings based on real data.
  • Linked downtime events to operational and changeover patterns.

Outcomes

  • Unplanned downtime reduced by 35% within the first phase of implementation.
  • More predictable daily output and improved planning accuracy.
  • Data-driven culture shift toward continuous improvement and Lean execution.
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